elmer fudd
Contributor
I've been away from SB for awhile now, but I've kept up on the vintage diving.
Anyway, the other day I stumbled into a great deal on three DH regs and one old SH. Two of the three, (RAM & DAAM), were working pretty well. The duckbills were long gone and the wagon wheel valves were bad, but other than that they breathed pretty nice. The other two, a blue label Healthways Scuba and a Voit MR12 had free flows.
Not having a spare Healthways valveseat, what I ended up doing was taking out the orifice, cleaning it up on the lathe with 0000 steel wool and then applying a smidge of fine valve lapping compound to the seat and pressing it up to the orifice for about 45 seconds while running the lathe. After cleaning and reassembling everything the free flow was completely gone and it was breathing tolerably. I won't say it was breathing nice because you have to suck quite a bit harder than you would with a RAM to get air. I'm guessing the cracking pressure is about 2.5", but I think that's due to a hard old diaphragm, the basic design and the fact that I haven't tuned it yet.
This wasn't the first fix that I tried. I originally tried just cleaning everything and replacing the o-rings, then shimming up the valve spring, etc... The thing that got rid of the free flow though was polishing both the orifice and the seat.
Since this worked out so well, I'm kind of wondering what other peoples experiences with this are.
Anyway, the other day I stumbled into a great deal on three DH regs and one old SH. Two of the three, (RAM & DAAM), were working pretty well. The duckbills were long gone and the wagon wheel valves were bad, but other than that they breathed pretty nice. The other two, a blue label Healthways Scuba and a Voit MR12 had free flows.
Not having a spare Healthways valveseat, what I ended up doing was taking out the orifice, cleaning it up on the lathe with 0000 steel wool and then applying a smidge of fine valve lapping compound to the seat and pressing it up to the orifice for about 45 seconds while running the lathe. After cleaning and reassembling everything the free flow was completely gone and it was breathing tolerably. I won't say it was breathing nice because you have to suck quite a bit harder than you would with a RAM to get air. I'm guessing the cracking pressure is about 2.5", but I think that's due to a hard old diaphragm, the basic design and the fact that I haven't tuned it yet.
This wasn't the first fix that I tried. I originally tried just cleaning everything and replacing the o-rings, then shimming up the valve spring, etc... The thing that got rid of the free flow though was polishing both the orifice and the seat.
Since this worked out so well, I'm kind of wondering what other peoples experiences with this are.