R
redacted
Guest
Air 2 DIY service - Lessons Learned
Picked up a spare Air 2 on ebay last week. While it seemed to work OK, it had more green than I was used to. Some was bits of kelp and other was corrosion. Not real bad, but since it also smelled like the last user may have been a harbor seal, I decided to a service kit to it.
It really was pretty simple for my first trip thru an air 2 but there were a few lessons some might benefit from.
1. It was pretty cruddy so I soaked it in clean soft water for a couple days to loosen thing up. Seemed to work OK.
2. In spite of some of the dynamic o-rings being in poor shape, it help pressure and breathed quite well. The o-ring on the exhaust button had set in the shape of a washer rather than an O-ring. And the o-ring on the orifice was cracking and stiff. It definately needed the service.
3. Removing the exhaust spider without the special spider tool was also fairly easy. I used a small screwdriver against one spider leg at a time to get it started. Once started, I continued to use the screwdriver getting about 1/4 turn each time. A little tedious but not bad.
4. The spring on the inflator button can be switched with the demand valve spring. But the wrong spring does not have enough strength to overcome IP so it can not be adjusted to stop freeflow. The longer spring is the demand valve spring. Lesson learned the hard way but it gave me a little more practice with disassembly & assembly.
5. Had a bit of trouble reassembling the demand valve (with the correct spring) in the housing and attaching the insert, lever, washer and nut. You could probably do it with 3 hands. This is where the spider tool would be very helpfull. I finally removed the orifice from the inlet tube and the LP seat from the demand valve (to avoid damage). I then cut a piece from the cap of a cheap pen to act as a spacer between the inlet tube and the housing. With the 3/4 inch spacer in place of the orifice, I screwed the inlet tube into the housing which compressed and held the spring on the demand valve and allowed me to assemble the parts under the locking nut and secure the nut. The LP seat is easily installed after this is done.
Picked up a spare Air 2 on ebay last week. While it seemed to work OK, it had more green than I was used to. Some was bits of kelp and other was corrosion. Not real bad, but since it also smelled like the last user may have been a harbor seal, I decided to a service kit to it.
It really was pretty simple for my first trip thru an air 2 but there were a few lessons some might benefit from.
1. It was pretty cruddy so I soaked it in clean soft water for a couple days to loosen thing up. Seemed to work OK.
2. In spite of some of the dynamic o-rings being in poor shape, it help pressure and breathed quite well. The o-ring on the exhaust button had set in the shape of a washer rather than an O-ring. And the o-ring on the orifice was cracking and stiff. It definately needed the service.
3. Removing the exhaust spider without the special spider tool was also fairly easy. I used a small screwdriver against one spider leg at a time to get it started. Once started, I continued to use the screwdriver getting about 1/4 turn each time. A little tedious but not bad.
4. The spring on the inflator button can be switched with the demand valve spring. But the wrong spring does not have enough strength to overcome IP so it can not be adjusted to stop freeflow. The longer spring is the demand valve spring. Lesson learned the hard way but it gave me a little more practice with disassembly & assembly.
5. Had a bit of trouble reassembling the demand valve (with the correct spring) in the housing and attaching the insert, lever, washer and nut. You could probably do it with 3 hands. This is where the spider tool would be very helpfull. I finally removed the orifice from the inlet tube and the LP seat from the demand valve (to avoid damage). I then cut a piece from the cap of a cheap pen to act as a spacer between the inlet tube and the housing. With the 3/4 inch spacer in place of the orifice, I screwed the inlet tube into the housing which compressed and held the spring on the demand valve and allowed me to assemble the parts under the locking nut and secure the nut. The LP seat is easily installed after this is done.